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I
managed to get through the Winter of 2000-2001 with my wood boiler, but
was not at all happy with the smoke and the 22% net delivered
efficiency. During the Fall of 2001, I decided to void my warranty in
the interest of science and made three basic modifications to the unit. First
was to line the combustion chamber with a refractory material.
I decided on "regular" firebrick for the bottom, back and
sides, and alumina fiberboards for the top baffles. I also
made a secondary combustion chamber by adding a false roof of the same
alumina fiberboard panels, supported by the firebrick sides. I did not add
a means for providing air directly to the secondary chamber, figuring I
would just increase the draft to give excess air in the primary chamber,
which would then carry through to the secondary chamber to oxidize the
smoke and other unburned gases. Finally, I added a chimney top draft
inducer with a variable speed motor control, so that I could adjust the
chimney draft anywhere from .02 inch to .15 inch W.C..
The
improvement was amazing. On
the first trial from a cold start, I had a net delivered efficiency of
42%, this even with a lot of heat taken up by the firebrick mass.
As in previous tests, I let the system cool down by operating the
house circulators until the water jacket temperature was back down to
120 degrees F. Since the firebrick was now warm, the second trial was
even better! I got at least
48% efficiency. I say
"at least" 48%, because at that point, the water temperature
had reached the set point on the aquastat, shutting down the draft
inducer and closing the intake damper.
Another
improvement was the delightful lack of smoke!
To be sure, while starting up, the boiler did smoke, as does any
wood fire, but once all the wood had "caught", it was possible
to adjust the draft so that there was no visible smoke.
I found that it was best to start with the draft at maximum until
the chimney stopped smoking. This
would usually take 20 minutes from a cold start, 5 to 10 minutes after
adding wood to a hot bed of coals.
After that, the best results were obtained by backing off the
draft to the point where I just started to get smoke and turn it up a
bit. The best efficiency
was obtained by adjusting the draft as the fire progressed, turning it
down to minimum when the wood was near the ember phase of the burn. If I
didn't feel like going out every half hour and fiddling with the draft,
the best compromise draft setting seemed to be .05" W.C. once the
fire was going.
I
did have some problems with the high heat cracking the original calcium silicate
panels, on the third trial, the false firebox ceiling and baffles
collapsed into the firebox. I had to wait half a day for everything
inside to cool down enough to safely handle. I
rebuilt the inside using alumina fiberboard panels and they have stood
up for three seasons now.
These
modifications reduced the amount of the wood that can be handled in one
load to about one half of original, but because of the improved
efficiency, the boiler will still go for about 6 hours before reloading
as before. On above
freezing days, I have to give it 3/4 loads, else it will cycle off and
I'll lose all the efficiency in a smoldering fire. I also found out that
very small loads (less than half) don't work well, as the temperature
never gets hot enough to light off the smoke and gases. One way to avoid
this problem would be to add a heat storage means, such as insulated
water tanks in the basement. That
way the unit could even run in the spring and fall at maximum efficiency
and little smoke.
Bob
in Pennsylvania
Footnote: Method of measurement of net delivered heat efficiency and
btu/hr.
The
system is known to contain 150 gallons of water.
Water weighs 8 pounds per gallon, for a water weight of 1200
pounds. The BTU is defined
as the amount of heat required to raise one pound of water 1 degree F.
The btu/hr rate was determined by timing how long it took to
raise the water temperature by one degree, under the test conditions
stated below. The boiler comes equipped with a digital thermometer with
a stated accuracy of 3%
The
net delivered efficiency was determined by loading the boiler with a
known weight of wood, typically 40 pounds. The wood for each trial was
red oak, cut from the same tree, seasoned and stored in the same manner.
Before each trial, ashes
and coals from previous fires were removed from the boiler.
The heat from the system was removed by allowing the house
circulators to operate until the boiler temperature was down to 120
degrees F. At this time,
the house circulators were turned off and the valves to the house
heating system closed. The
power to the oil burner was also switched off.
The circulator for the wood burner was left running, so as to
prevent stratification of the water inside the wood boiler. This method also inserted the transmission loss through the
piping system into the measurements, since the water circulated from the
wood boiler, to the house through the inactive oil boiler and back to
the wood boiler. There may have been some extra losses through the
inactive oil boiler, but these are believed to be negligible, as the
boiler was well insulated and the measured stack temperature of the oil
boiler while inactive was the same as the ambient temperature.
The wood was then ignited and allowed to burn until the boiler
temperature no longer showed an increase.
At that time the temperature was recorded.
The embers and unburned wood, if any were weighed.
The heat output was determined as detailed in the previous
paragraph. The input was
determined by multiplying the weight of the wood consumed by 6000 (an
average value stated for seasoned red oak).
Efficiency was determined by dividing the BTU output by this
input value.
Bob,
Pennsylvania, USA
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The original
firebox was steel surrounded entirely by a water jacket. You can
see how cold it ran by the black color and creosote clinging to
the steel. The first step was to use standard firebrick for the
floor.

More bricks line the sides and
rear and the top baffle was added. The baffles are made from alumina fiberboard
sheets.

Here is the false ceiling
installed. The exhaust leaves the firebox at the back of the false
ceiling, flows forward and does a 180° turn around the leading
edge of the top baffle and goes to the back of the boiler and out
to the chimney. Most of the heat transfer happens in this last run
to the exit.

The front baffle
encloses the secondary combustion chamber where the flue gases do
the 180° turn.


The refractory
bricks and panels run so hot the carbon
burns off.

Heat in the
firebox was so much more intense that the draft damper solenoid
on the outside of the door failed. Ceramic fiber board shields
were added to the door to protect it.

No smoke while in operation. |